Page 6 Volume 49-Issue 4
Len Buckel’s “Pecos Texas” Incident . . .
On June 12th , Len Buckel launched
forth on what has become an annual
trans-continental cross country to Lock
Haven, PA, to celebrate the J-3 Piper
Cub’s Sentimental Journey. His trip there
took 4 days and 32.8 flying hours and he
arrived on June 18th. Len participated in
the usual activities, exchanged stories with
the usual cast of characters and then
launched for home on June 24th.
The flight home involved dodging a
few thundershowers and he reached the
approximate half-way point at Pecos, TX
on June 26th. Checking evening weather,
Len noted that Pecos was in one of the
counties with a warning for severe thun-
dershowers that evening. He checked the
sky, which seemed to be clear without
clouds. He didn’t hear any wind during
the night, but the next morning he noted
that there were many tree leaves on the
ground around the motel.
Arriving at the airport, Len was star-
tled when he noticed his Cub wasn’t
where he had tied it down! It was gone!
Since Pecos is staffed 24/7, it was
thought that perhaps a member, hearing
the thunderstorm forecast, had rolled it
into a hangar. However, a quick check of
vacant hangars produced no joy. At that
point, all concerned thought the Cub had
simply blown away.
Len then checked the 1800 pound
rated nylon straps he uses for tying down
the Cub and found the tail strap appeared
to have been cut and was still attached to
the tie-down ring. Later, he noted that
short lengths of the webbing also re-
mained on the wing tie-downs. Len and a
couple of airport people jumped into one
of the airport cars and started looking.
You can imagine what Len must have
been thinking, that he was going to find
his Cub in a little round ball! They drove
down runways and taxiways looking for
it, expecting the worst. Len was already
thinking that he would have to rent a
truck to take the wreckage home.
Finally, at the west end of the field
they spotted the Cub! It appeared to be
upright at least and on its wheels. They
had to walk into the high brush to get to
at the plane, but hope surged when they
found the plane in amazingly good condi-
tion! It had been blown at least a good
one-half mile from its tie-down. On ex-
amination, they found that the left wing
tip was bent but the aileron was not hurt.
Len used EMT tubing for the wing tip
bow which probably kept the wing from
being damaged further inboard. The
right aileron had been in the dirt, but
apparently was not damaged. Both eleva-
tors sustained some damage, but other
than that, there didn’t appear to be any
further damage! They also noted that the
wing tie-down straps were still attached
to the airplane and had been broken near
the ground. There were about four peo-
ple on the scene at that point, and they
were able to push the Cub out to the
nearest runway. Len said he was truly
amazed that the Cub had not sustained
more damage.
Len then took it on a test flight
around the field, but other than being a
bit tail heavy, flying qualities were accept-
able. Then, as if to add a bit more insult
to injury, when Len taxied up after his
flight, the right tire went flat! The tire
was full of thorns from the brush area
where it had ended up. When the plane
was rolled out of the brush, they must
have collected the thorns. Len took the
tire to a nearby tire shop
where the technician re-
moved the tube and in-
stalled TEN patches. The
left tire remained inflated
until Len got back to San
Diego, then it too went flat!
After installing the re-
paired tire, Len decided to
try a full-power flight test
and if successful, would
depart for home. The Cub
seemed to fly all right with-
out any significant trim
problems or vibration so he set course
for home. Len’s remaining flight took
him through Deming, NM, Casa
Grande, AZ with his third landing at
Gillespie Field at 11:30AM on June
28th. Total flight time for his trip was
68.3 hours. That is indeed a long time
to sit in the back seat of a J-3 Cub
dodging thunderstorms.
There is no doubt that Mother
Nature smiled broadly in Len’s direc-
tion during the episode. Had only one
or two tie-down straps broken with
one or two holding, the airplane
would likely have gone on its back, or
worse, on top of its nearest neighbor.
There is some mystery concerning
why all three tie-down straps failed
near the bowline knot used to secure
them. Len feels that the nature of the
knot itself, may have contributed to
the tie-down strap failing. Len re-
ceived some information that knots
can reduce the effectiveness of tie-
down materials up to 40-50 percent.
Regardless of why they failed, it
was probably fortunate that they did,
since the Cub was saved as a result.
As noted in the photo below, Len is
already well underway repairing the
Cub. With any luck, it should be fly-
ing again by the end of August.
Ed. Note: A humorous cartoon drawn
by Sheldon Green depicting Len’s ordeal is
included on Page 8.
Len repairing the Cub’s left wing tip.